Front Fork Installation
The front fork installation is quick and easy to complete.
Tip#1
The fork can accidentally be installed 180 degrees off, there is a much larger lip on the "front" of the fork to help orient the part in relation to the nose gear tube.
Although not shown in the picture above, I deferred installing multiple parts to make the assembly easier to move around due the weight and size.
- Wheel and tire
- Wheel spat mounting brackets
Nose gear strut and engine mount
This part of the installation was time consuming for many builders and I was no exception.
The Vesconite bushings are cut in half on the lower bushing location and use an unmodified bushing on the upper mount.
The upper bushing fits firmly in the upper bushing mount, I used a rubber mallet to "gently" knock the bushing into place.
The upper bushing fit squarely and aligned with the upper hole in the engine mount as shown below.
The lower bushings must be sanded to reduce the turning force required to rotate the nose gear assembly.
I followed another builders recommendation (Patric Shine) and sanded using sand paper to enlarge the bushings.
I used 400 / 500 grit to slowly remove material then re-assembled and rotated the tube back and forth.
Using this method I could see where the tube was binding on the bushing and continued to sand until these areas were uniform across the face of the bushing.
The dowel method probably would have been faster overall but I think both methods get the same results.
This is another builders image, as I lost a number of pictures during a phone upgrade.
Here is another example by builder Olivier Mo:
With the Vesconite bushings sanded down and 800/1000 grit sanded back to a glossy finish I moved on to securing the bushings using the node gear bushing locking brackets. This is where things took a tune that I wasn't expecting, the brackets fit but threw the bushings out of alignment.
The lower split bushings, retainer brackets and bolts fit just fine, however; the upper brackets for the solid bushings would not fit with the bolts inserted.
You can see in the picture below that the alignment pin I was using and just how far the locking plate was from aligning with the pin.
If you tried to force the bolts in which I could do, it would change the alignment of the upper bushing resulting in excessive force required to turn the nose wheel tube.
I talked to the factory about it like many others have and the response was always to keep sanding the bushing.
After a many days of staring at the problem I began to suspect that the bushing wasn't the problem and I started looking at the slots where the locking plates insert around the bushing.
The upper locking plat inserted easily and without resistance.
The lower locking plate had to be forced in, which caused the bushing to shift from it's nature location in the slot.
I noticed there were several witness marks on the lower plate which lead me to look at the welds inside the locations highlighted below.
One both sides the welds were much taller and had a lot of slag on the mating surfaces.
Lightly cleaning up these welds and removing the slag from the mating surfaces completely resolve the locking plate binding issues.
Now that the bushing wasn't being twisted inside the mount the turning resistance was significantly reduce.
I still needed to sand the bushings because I could see witness marks on the inside the bushing where it was out of alignment.
Using a similar method to the lower bushing I started with 400/600 grit on the and kept reinstalling the bushings and brackets till I could see an even wear patter on the surface of the bushing. I cleaned up the bushing with 800/1000 grit paper until the insides were a shiny smooth surface.
The bolts were again installed to secure the bushing and plates and the force required to turn the assembly was minimal.